It was not a wing nut as i had thought. The nut and washer on the 3 & 4 side that holds the fan shroud had fell off and apparently was between the casting and the head and fell off in one of the ports. The bolt stayed on the back side of the valve and the washer went through. A friend of mine pulled the head off and retrieved the washer . He said he thought I would be alright.
We got the carb and everything on and when we started the motor I am getting nothing from the left side. Three and four haven't even tried to hit or anything. We checked the compression on 3&4. Good on both. Both are getting fire. Checked the valves on both and set them. Tried to adjust the timing while the motor was running on 1&2. Didn't make any difference. The plugs are not real wet. I don't think the casting on that side has a leak but not sure. I am using the 34pct and I just set it what the settings said which should be good enough for it to run I would think. Any suggestions. Thanks
We got the carb and everything on and when we started the motor I am getting nothing from the left side. Three and four haven't even tried to hit or anything. We checked the compression on 3&4. Good on both. Both are getting fire. Checked the valves on both and set them. Tried to adjust the timing while the motor was running on 1&2. Didn't make any difference. The plugs are not real wet. I don't think the casting on that side has a leak but not sure. I am using the 34pct and I just set it what the settings said which should be good enough for it to run I would think. Any suggestions. Thanks